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Sea Mills Burst Investigation Case Study

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Dec. 3, 2019
Courtesy ofInflowmatix

On the morning of Saturday 27th May 2017, an 8” cast Iron trunk main carrying water from a reservoir to the area of Sea Mills burst. The network isolation to repair the pipe resulted in loss of water supply to around 4000 properties between 12 and 30 hours, over the bank holiday weekend. Costs associated with the repair were estimated to be in the region of £8000 plus additional costs for water supply provision, regulatory penalties and negative publicity. Bristol Water needed to understand the contributory factors (i.e.network hydraulics, pressure related transients) in order to get to the root cause failure quickly and apply any lessons learnt to similar high risk scenarios.

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The network topology contained a pumping station, reservoir outlet valve and non return valve feeding two District Metered Areas (DMAs).Bristol Water chose to work with Inflowmatix to establish where pressure-related risks existed within their network and how these may have contributed to the pipe failure.

Solution
InflowSys™ Data Analytics Platform

Inflowmatix consulted with Bristol Water to establish the optimum location of 24 InflowSense™ high frequency pressure monitoring deployments. These captured high-resolution pressure data at 128 samples/second, significantly higher than a standard pressure logger or telemetry data (15 minute average) with analytics performed on the InflowSys™ platform.The results were displayed directly to the Bristol Water leakage team through the InflowNet™ application. A valuable metric captured and plotted was the Cumulative Pressure Induced Stress (CPIS™) index - a pipe stress index developed by Imperial College London correlating transients effects with pipe stress through fracture mechanics.